On Monday, the team met up and needed to address some of the issues that we had with the welder. Kevin was in constant communication with administration and Dan (from full-scale bogey) to ensure we were taking the correct course of action. Kevin and I took a trip to Praxair to retrieve a new tank of Argon for the remaining welds. After coming back and setting up the welder, I started and finished the welds necessary for the support structures. I encountered some issues during this process as I never found the correct way to properly weld these two components together due to the differences in thickness of the square tubing and the sheet metal. If I utilize too high of a current, the sheet metal would have a hole burnt through. However, if the current was too low, there would be no penetration of the square tubing. Even after completing 80 welds, this process was not mastered and still need to be cleaned up through other methods that will be looked into.
Last week, I ground down the welded support parts that attach to the track. I finished 20 of these parts and it required a lot of patience since grinding down steel requires some time. I even had a collet for the Dremel tool break on me since the diamond tip Dremel-bit pushed the collet to open up throughout the duration of the grinding process. By trying to close up the collet to secure the bit, one of the collet's prongs broke. After these parts were completed, I started drilling holes into them to ensure that they would fit into the whole track assembly smoothly. I used the drill press and some of the brackets that Kevin finished printing. The end result of these components looks like the following image: After the support structures were put together, we assembled the track fully for the first time. Although it was a small assembly that reduced the length of the track, due to removing several straights, it allowed for the other subteams to test the bogey and controls....
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