On Monday, the team met up and needed to address some of the issues that we had with the welder. Kevin was in constant communication with administration and Dan (from full-scale bogey) to ensure we were taking the correct course of action. Kevin and I took a trip to Praxair to retrieve a new tank of Argon for the remaining welds. After coming back and setting up the welder, I started and finished the welds necessary for the support structures. I encountered some issues during this process as I never found the correct way to properly weld these two components together due to the differences in thickness of the square tubing and the sheet metal. If I utilize too high of a current, the sheet metal would have a hole burnt through. However, if the current was too low, there would be no penetration of the square tubing. Even after completing 80 welds, this process was not mastered and still need to be cleaned up through other methods that will be looked into.
This week, I focused my efforts on cleaning up some of the welded sections that I worked on last week. Within the square tubing, there is a slight rise that follows along the length of the tubing. This makes it impossible for these parts to slide into the support sleeves that we have already made. In order to finish up these components, I filed them down with a combination of using a Dremel tool with a diamond bit tip and Spartan Superway's file. The first image shows the excess metal that protrudes out of the inside of the square tubing. The next image shows that same protrusion grinded down with the use of the Dremel tool and shop file.
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